Kwik Way 041

Post on 16-Apr-2017

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Transcript of Kwik Way 041

Kwik Way 041

Repair to the spindle lash clamp

The machine was purchased with the gearbox casting for the clamp broken and missing

I indicated the stripped gearbox on a Bridgeport and milled a shelf 1” wide.

An 1.5”X1.5X12” segment of A36 was machined in the approximate shape of the original casting

The A36 piece was drilled and doweled and attached to the gearbox with four 3/8”-16X1” SHCS, tapping directly into the gearbox casting.

The gearbox was then set up in a TA14 taking care to align the boring bar .003” high.

Original bore is 2.758. Removed .015” per cut until reaching 2.740”. At this point .002” cuts were made until tool bit cleaned a .010” wide area on the original bore adjacent to

the parting line with the new piece.

The gearbox then went back to the Bridgeport and the new clamp was split with a .0625” saw.

The ID in the gearbox had .0007” interference with the spindle sleeve. A .003” shim was added between the piece and the gearbox. A 2” travel dial indicator was attached to the

stop adjustment clamp to assist in defining depth of cut. The broken plastic fine feed wheel was replaced with a 4” aluminum wheel.